Was bored today so i decided to compound and wax the car , oh the joys of having a G220.
Had to have a wheel bearing changed this week and had a problem with the air-ride for the first time ever yesterday!!! Seems like the pressure switch got stuck due to a little bearing inside, luckily it righted itself again and is now working perfect once more. Phoned up Rayvern who did the system and he assured me it's no major thing and if it goes again to get a new switch for it, easy diy fix as well he tells me.
Basically there's a little tiny spring with a bearing on the top of it, this little spring is only about 5mm in width so it has hardly any pressure behind it. If a decent piece of muck gets in there or you don't empty your water trap regular (i do) then it can get stuck, so a good blast of wd40 to clear any crap and a decent blow out and we are riding perfect again.
Results of today's activities......
Better than ever, the hard work is paying off.